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Study and Practical Solutions to Reduce the Heat Load Air Cooler in unit 200 Bouali Sina Petrochemical Co. to Reduce the Flaring

Mohebbifar, Majid | 2017

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  1. Type of Document: M.Sc. Thesis
  2. Language: Farsi
  3. Document No: 50645 (06)
  4. University: Sharif University of Technology
  5. Department: Chemical and Petroleum Engineering
  6. Advisor(s): Farhadi, Fatollah
  7. Abstract:
  8. Inappropriate performance of the air-cooled condensers in the process industry will make the flow out of the air cooler not fully condensate and its pressure is greater than the design value. This will lead to product loss and safety issues. In this study, factors affecting the performance of air cooler and various solutions to solve these problems have been identified. As a case study, the first distillation tower of the Ali Siana Petrochemical Complex, which disrupts its function in some months of the year, has been investigated. Aspen Hysys process simulation software simulates the naphtha splitter unit and the Aspen Exchangers Design & Rating software simulates the air cooled condesor and study the various practical solutions. Finally, it has been suggested a series of recomendation. Installation of water coolers in the distillation tower overhead flow, the use of detergent in periodic cleaning, the use of magnetic filters to improve feed quality, and to reduce the pressure of the tower and the simultaneous use of the water cooler
  9. Keywords:
  10. Air Cooled Condenser ; Fouling ; Flare Gases ; Corrosion Inhibitors ; Overhead Corrosion ; Naphta Splitter Unit ; Process Analysis

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